REPOWERING HO SCALE TROLLEYS WITH A-LINE COMPONENTS
By George Huckaby & Joe Delia

June 1, 2002
Revised June 1, 2004

BACKGROUND

Since the founding of the Southern California Traction Club in 1995, the club has had to develop its own set of standards for the repowering of HO traction vehicles. This repowering activity has it roots in the club desire to operate five cars trains of Pacific Electric 1200s, or "Blimps" all powered.

In preparing for this train activity, it was immediately discovered that occasionally, open frame motors require up to one ampere to start. Our 4.0 amp Innovator throttles would not like that, even if another train or car was not in the same circuit. Then, after we located the Kato automatic couplers, developed a way to use them, (See Trolleyville Schoolhouse Lesson 1 in Room 4) and trained up some cars, it became obvious that the cars need to run at approximately the same speed. To our surprise, similar cars from similar frames of manufacture had widely differing speeds, although they all seemed to run smoothly individually. After several attempts, the club initially settled on the Sagami manufactured motors, initially using 22361-9 and 22340-9 motors. These motors with their 22 mm diameter and 2.4 mm shafts, were ideal replacements for the open frame motors. The 22361-9 motor was rated at 9800 rpm at 12 volts and .075 ampere. The 22340-9 was rated at 9800 rpm and the same voltage and ampere rating. The difference between these two motors in identical cars was noticeable but not a problem. The Sagami 22340-9 motor became the motor of choice except where space was a problem. The club was in the process of converting most of their Pacific Electric Suydam cars with these motors when they became unavailable. When this happened, the club desperately turned to A-Line's Joe D'Elia for help. A-Line was importing Mashima motors and produced a line of drive line parts so this seemed to be an excellent place to start. We discovered that the A-line 40321 motor was rated at 9500 rpm at 12 volts. So cars equipped with this motor would be compatible with those already repowered with the Sagami motors. Note the table later in this lesson comparing the various motors. But, the A-line motor had a 2.0-mm shaft versus the 2.4-mm shaft of the Sagami motors and the open frame motors that they replaced.

So after some adjustments, including the development of the 2.0 to 2.4 mm sleeve, we found the A-line motor to be an excellent performer. After many years, these Mashima motors have performed equal to or better than both the Sagami 22361-9 and 22401-9 motors.

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Motor RPM @ 12 VDC Current @ 12 VDC Vert Ht Wt (oz) Shaft
Sagami 22361-9 9,500 75 milliamps 22 mm 1.5 2.4 mm
Sagami 22401-9 9,800 75 milliamps 22 mm 1.8 2.4 mm
A-line 40321 8,500 90 milliamps 23 mm 1.4 2.0 mm
A-line 40322 9,200 80 milliamps 23 mm 0.9 2.0 mm
A-line 40324 11,000 70 milliamps 16 mm 0.7 Shaft
NWSL 20325-9 9,500 50 milliamps 20 mm 2.0 mm
Open Frame Motors Varied Varied Varied 1.4 to 2.9 oz 2.4 mm

As a result, the SCTC has developed a method of repowering most of the spring belt drive cars with A-line motors and flywheels and most of them run like Swiss watches. As usual, there were tradeoffs. The Mashima motors were 33mm high, which was no problem in the PERy interurbans but this height made them hard to fit, if not impossible to use, in some of the smaller streetcars. Original open frame motors were only 22mm high including the brush holders, so there could be problems with the 40321 motor.

Note: At this time, we still prefer the A-line 40321 motor but so far the NWSL 20325-9 motors have been adequate. The lone 40324 motor so far used has also performed well, running for eight hours at a time on the Custom Traxx traction demonstration module at shows. As soon as any new motor appears on the scene that has traction applications, we will be trying these also.

Many fine HO scale streetcar models were produced in the 1960's and 1970s by such firms as Fairfield, Model Tramway, S. Soho and Company and Pacific Traction. These cars all have some similar traits. They have excellent brass bodies, crafted of very solid brass, open frame motors and, usually, spring belt drive. Several of these vintage models, some of which have never been run, have been offered for sale lately, especially on Ebay. In December 2001, we obtained a pristine Orleans 800-class streetcar, 300 of which were imported in 1965 by Fairfield Traction Models. Repowering this model is the subject of this article. We also had a model of the Brooklyn 8000 series Peter Witt car, 500 of which were imported by Fairfield in 1970. Repowering it required changes due to less vertical room inside the car body. We will refer to those changes later in the article. Otherwise the method used is the same as the New Orleans car.

We do not present this method as the only way to repower or the best way to repower. Some readers may have a vastly superior method of repowering cars, but, as of this writing, these methods have not been shared with the Trolleyville Schoolhouse editors.

The repowering method that we will describe in this lesson will work in the majority of all brass double truck interurbans and many streetcars. For those cases, ingenuity is the order of the day. But for the majority of HO scale electric vehicles, below are a list and a photo of all the items that you would need for such a successful repowering. The list of parts includes the following:

1 - A-Line 40321 18mm by 33mm flat can motor

(Alternates are NWSL 20325-9 motors with 9500 rpm rating)

1 - A-Line 20006 flywheel (Cylinder)

(Alternates are A-Line 20021 flywheel (Trapezoid Shaped)**)

1 - Original Motor Pulley (removed from original motor shaft)

1 - A-Line 12053 2mm to 5/32" sleeve

1 - A-Line 12401 Motor Cradle

1 - A-Line 20010 Flywheel Cement ***

1 - Tube DAP DOW Corning Clear 100% Silicone Clear Aquarium sealant

*used when interior height does not permit use of the 40321 and shown in the photo below.

**used when space does not permit use of the 20006 flywheel.

***used to affix the 12053 sleeve and the 20006 flywheel to the motor shaft and shown in the right photo.

The next two photos are of the New Orleans car, right out of the box and then the power chassis with the body shell removed.

Before we removed the body shell, we gave the entire unit a thorough two-rail test. This was to ensure that the wheels are in gauge and that there was no problem with the power truck. One of the problems with spring belt drives is if they have been idle for a long period of time, they will sometimes end up with an almost permanent bend in the belts where they were wrapped around the upper and lower pulleys. These spots will either work themselves out after a period of operation or they will have to be replaced. If the belts have really deteriorated, they will break and have to be replaced anyway. Replacement belts are available from Alpine Division Scale Models, PO Box 6, Artesia, CA (562) 860-6060. Replacing these belts is a topic that is not covered here. It is not difficult but it takes patience.

PROCEDURE

STEP 1. The first step is to measure the distance between the original horizontal motor shaft and the car floor. Record this distance, as you will want to attempt to maintain this distance, if possible, with the replacement motor shaft.

STEP 2. Now remove the old motor from the car floor and all mounting hardware. Unsolder all motor connections to the floor, the rear truck and any other connections, if they exist. Clean the floor carefully and thoroughly, as you will be using adhesives to hold the motor and or cradle to this floor later.

STEP 3. Remove the motor pulley from the old motor by loosening the setscrew. Set the pulley aside. You will use it on the new motor.

STEP 4. Take the 12053 sleeve and place it on the 40321 motor on the same end as the electrical connections. Place only 2/3 of the sleeve on the shaft and secure with the 20010 flywheel cement.

Note: Some modelers have used a small dab of ACC to secure sleeves and flywheels. This can have serious consequences if the parts turn out to be in the wrong place and must be re-positioned. Also a little bit an errant ACC can get into the motor bearing and completely ruin the motor. We feel that A-line Flywheel Cement is much more suitable for this role. The A-line 40321 and 40322 motors have motor shafts that are much shorter than the open frame motors or the Sagami motors that were initially used. The original open frame motors and the Sagami motors all had 2.4 mm motor shafts. The original motor pulleys were designed for these 2.4 mm shafts. The A-line motor 2.0mm shafts require the use of the #12053 sleeves. These sleeves were developed by Joe D'Elia at the request of the club just for these repowering efforts.

STEP 5. Install the 20006 flywheel on the motor shaft opposite the pulley as close to the motor casing as possible. Use the 20001 flywheel only when there is insufficient room for the 20021. Both the 20006 and 20021 flywheels are designed to fit a 2.4mm shaft without use of the 12053 sleeve.

STEP 6. Install the 12401 cradle as close to the power truck as possible, ensuring that the cradle does not foul the swinging truck or the worm gears.

Ensure that the cradle in centered on the chassis and parallel to the sides of the chassis. In some cases, there are screws holding underbody equipment that will interfere with the flush mounting of the cradle. Because of the soft metal used in the cradle, it is relatively easy to file the cradle to accommodate the screw. The cradle has been designed with a concave radius, which approximates the radius of the curved sides of the motor. This helps get a good seal with the motor when the motor is finally cemented to the cradle. The cradle also helps make up the loss in weight from the heavier open frame motor. Current practice is to use Aquarium sealer but other adhesives such as Pliobond, Walthers Goo or even double-sided tape could also be used. Remember that the use of tape will increase the height of the motor cradle combination inside the car and could pose a problem.

Due to the low roofs of some city cars, such as the Brooklyn car and the chassis shown next, we could not use the cradle with the 40321 motor.

The motor-cradle combination was too high to fit inside the car. The motor occasionally contacted either the roof or the printed circuit strips used for the interior wiring. Despite the fact that we were so pleased with the performance of the Mashima 40321 motors, we elected to use the Northwest Short line 20325-9 round can motor in order to maintain the weight and center-of-gravity advantages of having the A-line 12401 cradle.

After the original lesson was written, we began experimenting with the Northwest Short Line 20325-9 motors, also rated at 9500 RPM. This experiment was begun after the weight and low center of gravity advantages of using the cradle was being discovered. The weight and the location of the cradle have significant effect on car performance through sharp curves and turnouts. The open frame motors that we were replacing weighed between 1.4 and 2.9 oz. The A-line 40321 motor weighs 1.4 oz; the 40322 motor 0.9 oz and the 40324 motor 0.7 oz. In the original conversions in Suydam Pacific Electric 1200 series cars, there was little or no weight loss with the replacement of the motors with the 40321. There was also plenty room inside the car for the A-line 40321 with the 33.0 mm height and any additional weight needed. The 40321 was not going to fit inside the low roof of this many city cars. If the motor did fit, it occasionally contacted the roof of the car, resulting in excessive noise during operation.

In the original lesson, we fashioned a special mount for the motor using rubber and fit the motor into the car. After some running time, the car did not perform as expected. The car needed additional weight to track well through city curves and specialwork and there was little room to place it. It was here that we discovered the true excellence of the A-line cradle. The cradle placed 1.0 oz of weight exactly where it was needed. Streetcar models are smaller and weigh much less than interurban cars. The average remotored Suydam PERy 1200 was 11.5 oz while the highest weight of a Double End Peter Witt Car with cradle was 7.1 to 7.4 oz. Weight of these smaller cars is much more critical, especially since the drag of the trolley pole will have to be overcome in operation. Since the use of the A-line cradle, with its 1.0 oz weight, satisfied that need, we went looking for another motor that would fit both on the cradle and inside the car. The A-line 40324 motor, currently available, was not available at the time of these conversions, so we used the NorthWest Short Line 20325-9 motor, which had a height of only 20mm. This 20325-9 motor also has 2 mm shafts, so use of the 12053 A-line sleeve was also required. The NWSL motor was then affixed to the cradle using Aquarium sealer. The specific car used for this remotoring method, a Fairfield Brooklyn 8000 series Peter Witt, numbered 8125, was certified by the SCTC for operation at 30 scale miles per hour (smph) at 7.0 volts. Since that time two other identical Brooklyn Peter Witt cars have been so converted. They certified between 28 and 30 smph each. The completely converted chassis with A-line motor 40321, cradle 12401 and flywheel 20006 is shown in the next photo:

Two more identical cars were so converted about one year later and certified at the variance being due mainly due to the difference in tensions of the spring belts.

Again, because we were so pleased with the performance of Mashima motors, we decided to test the new A-line 40324 motor, when it became available. There was no way to fit the A-line 40321 motor into a Custom Brass Third Avenue Railway System 400 series semi-convertible due to the inward curving sides. The 12401 cradle could not be used. At that time of this article, the 2003 A-line catalog shows 14 cradles, stock numbers 12400 through 12413, that were originally intended for re-motoring of Athearn and Rail Power Products diesel locomotives.

Note: We normally mount the cradle to the frame with DAP Aquarium sealer. In most cases, we must file some of the cradle away to clear some of the screws holding underbody equipment. After waiting at least six to twelve hours, we will then mount the motor to the cradle. As of this date, we have not have either a cradle or motor work its way loose.

Twelve of these cradles are shown in the next photo.

We found the 12401 cradle works in most traction repowering applications. But in the case of the TARS car with its narrow body, we had to modify another cradle, the 12400 by removing the winged sides so that the cradle and motor should fit inside this body.

This motor also has 2.0 mm shafts, so use of the 12053 A-line sleeve was also required. This car also certified at 26 mph, a perfect speed for the SCTC city modules.

STEP 7. Take the motor-sleeve-pulley combination and place it in the cradle such that the two knurled portions of the pulley are directly over the similarly knurled pulley in the power truck. Ensure that the horizontal distance between the motor shaft is the same or slightly greater than the measurement taken earlier.

Note: At this time, it is best to make the electrical connections to the motor as it will be difficult to solder to the lower terminal once the motor is secured to the cradle.

Note Electrical connections are discussed thoroughly in a separate lesson on Wiring Trolley Cars for Overhead Wire Operation.

The SCTC uses trolley pole reverse and overhead wire power so Miniatronics #50-001-02 2-pin connectors are used to connect the motor to the chassis. At this point, the female end of the connector is attached to both motor leads. Normally, the white striped wire is connected to the '-' lead of the motor and eventually to the rear trolley pole pivot. But testing before final assembly is prudent.

STEP 8. At least six hours after the cradle was secured to the chassis with DAP Dow Corning Aquarium sealer, secure the motor to the cradle using the Aquarium sealer. Place some sealer in the middle of the cradle as shown below:

STEP 9. Press the flywheel - motor - pulley assembly into the aquarium sealer. Line up the two pulleys and clean up the excess sealer that will seep out from under the motor. Do not allow the sealant to attach itself to the flywheel. Do not allow the sealant to get into the worm gear of the power truck. Allow the sealant to cure at least twelve hours before attaching the spring belts.

Note: Pulleys were imported in various sizes from about 7.0 mm to 9.0 mm. Adjustments in speed can be made by changing pulleys. The larger the pulley, the faster the car, all other things being the same!

STEP 10. Once the sealer has cured, reattach the spring belts, paint the flywheel and pulley flat black. Finish all chassis painting, reattach to the body both physically and electrically and the repowering is completed.

This car, still unpainted at the time, ran its first miles at the All Brass Show in Ontario on January 20, 2002 and has been running fine ever since. Since then four more similar cars have been converted, painted and finished. The current fleet of the five Brooklyn cars is shown below:

Happy Conversions!